fix [3369027] Sensor.TYPE_ROTATION_VECTOR is unstable and returns NaNs when running slowly
The cut-off frequency of the lowpass filter was too high for the sampling rate used by DELAY_NORMAL. Now we use the same filters used for the gravity vector (cascaded biquad at 1.5 Hz) Change-Id: I319dc4f449a3abd553d61b196a9ddcf7782f912d
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