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Commit 772aed45 authored by Felipe Contreras's avatar Felipe Contreras Committed by Felipe Balbi
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usb: musb: fix pm_runtime mismatch

In musb_init_controller() there's a pm_runtime_put(), but there's no
pm_runtime_get(), which creates a mismatch that causes the driver to
sleep when it shouldn't.

This was introduced in 7acc6197[1], but it wasn't triggered in my setup
until 18a26892[2] was merged to Linus' branch at point df0914[3]. IOW;
when PM is working as it was supposed to.

However, it seems most of the time this is used in a way that keeps the
counter above 0, so nobody noticed. Also, it seems to depend on the
configuration used in versions before 3.1, but not later (or in it).

I found the problem by loading isp1704_charger before any usb gadgets:
http://article.gmane.org/gmane.linux.kernel/1226122

All versions after 2.6.39 are affected.

[1] usb: musb: Idle path retention and offmode support for OMAP3
[2] OMAP2+: musb: hwmod adaptation for musb registration
[3] Merge branch 'omap-for-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/tmlind/linux-omap-2.6



Cc: stable@vger.kernel.org
Cc: Hema HK <hemahk@ti.com>
Signed-off-by: default avatarFelipe Contreras <felipe.contreras@gmail.com>
Signed-off-by: default avatarFelipe Balbi <balbi@ti.com>
parent e7f4e732
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+0 −2
Original line number Original line Diff line number Diff line
@@ -2013,8 +2013,6 @@ musb_init_controller(struct device *dev, int nIrq, void __iomem *ctrl)
	if (status < 0)
	if (status < 0)
		goto fail3;
		goto fail3;


	pm_runtime_put(musb->controller);

	status = musb_init_debugfs(musb);
	status = musb_init_debugfs(musb);
	if (status < 0)
	if (status < 0)
		goto fail4;
		goto fail4;