Donate to e Foundation | Murena handsets with /e/OS | Own a part of Murena! Learn more

Commit 94bef000 authored by Matt Ranostay's avatar Matt Ranostay Committed by Jonathan Cameron
Browse files

iio: hudmidity: hdc100x: fix incorrect shifting and scaling



Shifting sensor data to the right 2 bits was incorrect and caused the
scaling values + offsets to be invalid.

Reported-by: default avatarAlison Schofield <amsfield22@gmail.com>
Signed-off-by: default avatarMatt Ranostay <mranostay@gmail.com>
Tested-by: default avatarAlison Schofield <amsfield22@gmail.com>
Cc: <Stable@vger.kernel.org>
Signed-off-by: default avatarJonathan Cameron <jic23@kernel.org>
parent 590b92a3
Loading
Loading
Loading
Loading
+8 −8
Original line number Diff line number Diff line
@@ -164,14 +164,14 @@ static int hdc100x_get_measurement(struct hdc100x_data *data,
		dev_err(&client->dev, "cannot read high byte measurement");
		return ret;
	}
	val = ret << 6;
	val = ret << 8;

	ret = i2c_smbus_read_byte(client);
	if (ret < 0) {
		dev_err(&client->dev, "cannot read low byte measurement");
		return ret;
	}
	val |= ret >> 2;
	val |= ret;

	return val;
}
@@ -212,17 +212,17 @@ static int hdc100x_read_raw(struct iio_dev *indio_dev,
	case IIO_CHAN_INFO_SCALE:
		if (chan->type == IIO_TEMP) {
			*val = 165000;
			*val2 = 65536 >> 2;
			*val2 = 65536;
			return IIO_VAL_FRACTIONAL;
		} else {
			*val = 0;
			*val2 = 10000;
			return IIO_VAL_INT_PLUS_MICRO;
			*val = 100;
			*val2 = 65536;
			return IIO_VAL_FRACTIONAL;
		}
		break;
	case IIO_CHAN_INFO_OFFSET:
		*val = -3971;
		*val2 = 879096;
		*val = -15887;
		*val2 = 515151;
		return IIO_VAL_INT_PLUS_MICRO;
	default:
		return -EINVAL;